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Refrigeration Repair
Underway
7/31/03
Blaine Parks
(previously published in Blue Water Sailing)
Back in
May of 2000, Janet and I had invited some two hundred friends and family members to
our home for a bon voyage party. The event was a huge affair with tents, a
live band and plenty of food. The party marked our last hurrah on land -
our house would be cleaned out the following day - so we emptied the
refrigerator and freezer, cooking everything to prevent throwing it away.
It was a real feast. Now as we motored through the Dismal Swamp Canal
aboard Charbonneau two years later, I was envisioning another feast. Only
this time we would be serving food to complete strangers as fast as we
could cook it because Charbonneau's refrigeration system had inexplicably
quit working. Unless I worked fast, all our frozen food - a full
six-month's stores - would spoil.
The day
before, our cold plate refrigeration system was the cornerstone of cooling
bliss. It had worked flawlessly for the previous 12,000 miles, right up
until this morning when I flipped on the breaker and nothing happened.
While cruising, we run the system for 90 minutes each morning to 'charge'
the cold plates. The temperature inside the box then stays at an
acceptable level until the following morning when we repeat the process.
Now, more than 24 hours since the last run, it was a race against the
clock to find and repair the problem before our food thawed.
I should
acknowledge that I was mechanically inept prior to cruising. After two
years of cruising, my skills have improved markedly. In fact, I've come to
thoroughly understand most systems on our boat; my education usually
peaking right after they fail. This, however, would be my first lesson in
refrigeration repair.
Our Crosby
refrigeration system -- a traditional ½ horsepower water-cooled,
belt-driven DC motor and compressor with two holding plates -- is located
underneath the galley sink and pushed as far outboard as possible. The
sight glass and service valves are accessed through a cabinet door under
the sink. Reaching the business end of the system, the motor and
compressor, requires squeezing my 190 pound body into a 15" x
12" opening in the galley's countertop. It is a very tight fit.
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Blaine
dives in to get a better look at the problem
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Charbonneau's
12-volt Crosby refrigeration system
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Cruising
is often defined as fixing your boat in exotic locations. I disagree
because it didn't seem very exotic as I hung upside down, suspended
through that small opening in our galley's countertop. The view from where
I precariously dangled offered no sunset views, no swaying palm trees, and
no peaceful anchorages. All I saw were twists and turns of copper
refrigeration tubing connected to various pieces of equipment I'd never
seen before. Nigel Calder's book, Boatowner's Mechanical and Electrical
Manual, helped me identify the parts. That was important so I could cuss
and call each piece by name as they took turns bloodying my knuckles.
Running through my mind were questions like, "Why wouldn't it run,
which hidden part holds the secret to this motionless beast, and will I
die upside-down, stuck in this little hole?"
The
symptoms were simple. The unit remained motionless with the breaker in the
'on' position, but there was a slight current draw showing on the
electrical panel's amp meter - around 5 amps where 45 amps is normal at
start-up. I also heard a faint 'thump' near the unit each time the breaker
was switched from off to on. While I was troubleshooting the system, Janet
called down from the helm saying, "The water pump seems to be working
and the discharge water flow looks normal. Maybe the amp draw is from the
water pump." I agreed and continued my inspections while she steered
Charbonneau along the narrow, tree-lined canal. Adding it up, I had a
lifeless motor and a faint thumping noise. Not much to go on, but at least
the water pump was working.
Experience
with previous equipment failures led me to check for blown fuses or loose
wiring connections first. Hoping for a simple solution, I checked the one
7½-amp fuse mounted on top of the system's wiring control box. The fuse
was intact. It was time for the multi-meter.
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Checking
fuses is always a good first step - no problem here.
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Progressive tests with the multi-meter showed acceptable voltages from the
electrical panel to the control box and at each connection point inside
the box. I continued to follow the circuit from the control box to the
motor and found 13.2 volts at every test point, indicating no discernable
voltage drop between the control box and the motor. All the connections
looked good and showed no signs of corrosion at their terminals. So why
wouldn't it run?
Telling
Janet what I'd found, she suggested I dig out the owner's manual. Like
most men, reading the instructions had yet to occur to me. I was
encouraged when I saw that my actions were in line with those described in
the troubleshooting guide. I did, nevertheless, find one test I hadn't
tried - bypassing the high pressure shutdown switch.
The wires
providing DC power for the motor are routed through a high pressure
shutdown switch. This switch interrupts power to the motor if a high
pressure condition exists. It could also interrupt power if the switch
were faulty. I needed to test the motor by bypassing the switch.
Fortunately, the switch was wired with easily disconnected male and female
connectors. I disconnected the two leads and linked them together with a
short piece of 12-gauge wire, effectively bypassing the switch. With the
jumper wire in place, I crossed my fingers and pushed the circuit breaker
to the on position - no luck. I checked for power at the makeshift jumper
and found the motor was getting the full 13.2 volts. I felt I was getting
closer to discovering the problem, but our food was also getting closer to
thawing.
The
voltage readings were normal at every junction from the circuit breaker to
the motor and the pressure switch appeared to be working; yet the motor
wouldn't run. I dreaded the thought of working on the motor while being
inverted and stuffed inside that small opening. Removing the motor and
then working on it was a better idea, but not by much. I postponed the
inevitable by investigating the 'thumping' noise first.
It turned
out that the faint thumping noise was coming from the unit's solenoids.
Reading some more, I learned that the solenoids regulate power to the
unit, operating like valves opening and closing depending on the box's
temperature and thermostat settings. Our unit has two -- one for the
refrigerator and one for the freezer. Using the multi-meter I found them
to be working fine and engaging the circuit, indicating that the box
temperatures were below the thermostats' minimum settings. It was another
dead end.

Consulting
the boating bible - Nigel Calder's Boatowner's Mechanical &
Electrical Manual |
Taking a
break, I surrounded myself with every how-to book on the boat and
refocused my attention on the motor. What had I overlooked? Electrically,
the only things left unchecked were the motor's commutator and the two
brushes. The commutator is a ring of copper bars connected to the motor's
armature and field windings, which turn the motor when magnetically pushed
or repelled by an electric charge. The graphite brushes pass that electric
charge to the system by 'brushing' against the commutator. I know that's a
mouthful; I had to read three different books before I understood the
process. But it was important to understand how power was applied to the
motor once the wires disappeared into the motor housing.
I decided
to start with the brushes because I could remove and inspect them without
removing the entire motor. The unit's two graphite brushes are reached via
two access panels located on opposite sides of the motor housing. Each
access panel has two screws, top and bottom, holding a cover in place. By
loosening the lower screw a half turn, I found I could remove the top
screw and then rotate the cover to reach the brush housing. Each brush was
pressed against the commutator by a spring device, which was held in place
by a locking spring holder.
Removing
the brushes, while upside down, was tedious work. I looked like a large
fish with its tail hanging from a pelican's mouth - my feet kicking in the
air as I tried to climb further inside. Once inside, the first spring
holder was easily released by pushing it in and sliding toward one side;
however, since the spring was no longer under pressure, it suddenly took
flight. After spending several worrisome minutes tracking down that first
errant spring, I was much more cautious with the other side.
The next
step, with both the springs and their holders removed, was to remove the
wires connecting the brushes to the motor housing. Each brush has a wire
molded into its body and was connected to the motor via a small screw
terminal. There were two wires on this terminal; the one leading from the
brush and another leading from the power input leads. The design was
identical for both brushes.
The trick
was to remove each brush wire while not disturbing the power leads. It was
a trial and error process, but I found that the power leads were
terminated with a ring connector and the brush wires used a spade
connector, open on one side. This allowed me to loosen each terminal screw
a few turns and carefully slide off the brush wire, leaving the power lead
attached. The brushes simply slid out of their housing after these wires
were disconnected. Once both brushes were removed, I went searching for
the spare refrigeration parts carried aboard for just this occasion. It
also gave me a chance to let the blood drain from my head back down to the
rest of my body.
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A new
graphite brush shown (left) beside the old, worn one (right)
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Graphite
brushes are worn away over time by their constant contact with the
spinning commutator. The brushes I removed looked a little worn, but it
was hard to tell just how much until I compared them with the new ones.
When placed side by side, it became obvious that this could be the
problem. The old brushes were only a third the size of the new ones. I had
learned from rebuilding previous motors that brushes should be replaced
before they have worn away half their surface area. These were well past
that point. Armed with new brushes I climbed back into the hole.
Replacing
the brushes was a reverse of the removal process. Each brush was inserted
into the long slot that holds it in place. Being careful to not crimp the
brush wire unnecessarily, I inserted the spade connector underneath the
small screw terminal and tightened it. I then placed the spring in its
place, perpendicular to the brush. With the spring in place, I attempted
to reinsert the spring holder. It took several tries to install the spring
holder. The technique required placing equal pressure on both the top and
bottom of the spring while inserting the holder; tiresome but doable even
while inverted with a small flashlight in my mouth. After completing both
sides, I checked my work, closed the access panels, tightened the lower
screws and replaced the top screws removed earlier.
Once again
I crossed my fingers and reached for the circuit breaker. I heard the
'click' of the breaker and was immediately surrounded by the sweet sound
of the belt turning, the motor rumbling, and water coursing through the
cooling lines. It didn't match the serene sounds of the Dismal Swamp Canal
that Janet had been enjoying from the cockpit, but it sounded like a love
song to me. I had solved another mechanical mystery aboard Charbonneau.
Our
refrigeration system doesn't seem as incomprehensible now that I know a
condenser from a receiver from a filter/drier and can identify the other
parts attached to them. The troubleshooting process was straightforward
and helped me recognize which elements of the system were working and
which required closer inspection.
Don't fret
the next time your marine refrigeration system refuses to work; you're
probably more qualified to fix it than you think. Take your time, be
methodical, and follow each possible avenue for the failure. You may
ultimately need to call in a professional, but most problems are within
your grasp and resolving them is a gratifying facet of cruising. This
particular repair was accomplished with four simple tools: multi-meter,
screwdriver, flashlight, and mirror. I imagine every boat would have those
tools aboard.
Though
happy to have the problem solved, a small part of me wished I had failed.
After all, not fixing the refrigeration system might have resulted in one
heck of a cookout. As I put my tools away, my face was still a mixture of
bright red from hanging upside down and black streaks from working with
the graphite brushes. But when the sense of accomplishment settled in, I
broke into a huge dimple-to-dimple smile and yelled up to Janet, "Let
there be ice!"
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